We Revived This 1962 Morris Mini Cooper Barn Find!

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For the past 4 years, we’ve been slowly going through this very special barn find. If you’ve been following the site over the years, you might have seen a post or two about it. Running Barn Finds takes up the majority of my time, but whenever I get the chance to wrench on one of our projects, I take it! So, it’s taken a little longer to get it back on the road than we would have liked, but I recently put in overtime and got it going. Boy, is it hilarious to drive with its tiny 10-inch wheels, quirky 997-cu in 4-cylinder engine, and go-kart-like handling. We didn’t give it a full restoration, as we didn’t want to take away too much from its originality, but we went through all of the mechanical systems, and it drives great now!

I will try my best to cover all the work I’ve done over the past 4 years, but I might miss a few things, given how long it’s taken to finish. So, I’ll start with the big things. I dropped the entire front subframe and drivetrain. The engine and transmission were removed from the subframe so that I could service the axles, replace seals, and repaint everything.

The subframe was in excellent condition, so I stripped everything off of it and repainted it with chassis paint. I did my best to save any original components I could, like the control arms, with the plan to replace only those that really needed to be.

While the engine was out, it was decided to inspect and service the entire drivetrain. Since it’s a challenge to service the axles and input flanges with the engine in the car, or even in the subframe, I rebuilt the flanges and axle joints while it was out. As things were cleaned, they were repainted in two-part enamel paint in the correct Morris Motors green. I also removed all the auxiliary components and carefully degreased the engine and transmission. Prior to painting and reassembly, I performed a leak-down test and found that the center two exhaust valves were leaking, so I removed the cylinder head for machining. This sent us down an interesting road and accounted for nearly a year’s delay.

Once the head was off, I took it to a nearby cylinder head shop that specializes in race engines. They were confident they could rebuild it, but after several months, they admitted they couldn’t find the correct exhaust valve seats and offered to regrind the head. Since this engine was built to run on leaded fuel, we wanted hardened seats. I spent an afternoon calling parts suppliers and found the correct size. At this point, we weren’t feeling too confident about this particular shop, so I took the head and parts to a different shop.

Test fitting the new valves

The next shop was willing to take the job on, but once the seats arrived, they admitted they lacked the correct-sized tool to cut them. They contacted their tool supplier, who promised to deliver the needed tool in a few weeks. Fast forward several more months, and the tool supplier admitted that the tool had to be made in England and would take up to a year to deliver. This shop suggested we check with one of the other cylinder head shops in town that uses a different tool supplier. That shop would have to order the tool too, but it would arrive in a few weeks. Well, several months later, the tool finally arrived, so I dropped the head off, and they got to work. They cleaned the head, decked it, cut and installed the new hardened valve seats, new valve guides, and installed new valves with new springs and retainers.

The finished product was honestly worth the wait. It turned out beautifully and can now run on unleaded gas. Before putting the valvetrain together, I degreased the head and primed it. Once the paint had cured, I finished assembling the head and reinstalled it on the block using a new head gasket and studs. Once it was together, I performed another leak-down test, and the numbers were good.

I did a final degreasing and painted the entire engine. After several coats of paint and a few days of curing, it was ready for a new rear main seal, clutch, flywheel, and throwout bearing. With those in and the clutch cover on, it was ready to go back into the subframe, which proved trickier than expected. I was working alone that day, so getting the axles guided into the frame as I lowered the engine into the cradle was interesting, but I got it done without scratching anything or losing a finger (win-win, right!).

With all these delays, I had had plenty of time to bench-test parts like the starter, alternator, and radiator, all of which were bad, so new units from England were already on the shelf waiting to be installed. Since all the parts were ready to go, assembly moved along nicely. Prior to bolting the subframe and drivetrain together, I installed new copper hardlines for the front brakes and new hoses. I also cleaned up the firewall and installed new master brake and clutch cylinders. With that done, everything was bolted together using new mounts, rubber-bits, and hardware. Reinstalling the drivetrain went smoothly until I realized the brake line to the rear brakes can only be replaced with the engine out, so I lowered the engine back down and replaced it. Finally, the engine was back in.

With the engine in, I was finally able to test-fire it, and it started up. At that point, the only exhaust component installed was the new header, so it was extremely loud, but it sounded like pure joy to me. Since the original exhaust system was rusted out, we ordered a full replacement and decided to go with one that exited out the left side rather than the middle. While the center exhaust looks cooler, it’s louder, and we wanted to be able to drive this without destroying our hearing. Before the muffler went in, I dropped the rear subframe to rebuild the suspension and install new mounts. The original brake backing plates were retained, but the drums, shoes, cylinders, and wheel bearings were replaced. The frame itself was cleaned and repainted, so that it stays rust-free for years to come. I also installed new rubber cones and adjustable Spax shocks (the original Spax shocks were retained and can be rebuilt if the next owner is so inclined). Getting the rebuilt subframe back into the car was tough, as the new rubber mounts didn’t want to fit, but after lots of adjusting, it finally went in smoothly.

Once the back was finished, I installed the exhaust system and a new SU fuel pump, then returned my attention to the front end. While most of the front suspension was reassembled before installing the drivetrain, I still needed to rebuild the front brakes and install the new shocks. The brakes proved to be another major challenge. Early Coopers used 7-inch front disc brakes. Since most people upgrade to the later 7.5-inch models, getting replacement calipers is impossible, and because the car still retains its original brakes, we decided to keep them. A set of replacement pistons and a set of seals were sourced from England. Thankfully, the pistons weren’t seized, so the calipers were easily rebuilt. Finding new brake pads proved problematic, though. Replacement rotors are readily available, but the pads are no longer being made. An alternative part is available, but it requires the calipers to be machined for the pads to fit. While that was a reasonable option, there was actually a box of spare parts in the car’s trunk, and wrapped inside was a set of new-old-stock pads!

With the brakes working and the suspension all together, we were finally able to lower the car back onto the ground. When we got the car, it was riding on its original steel wheels with old snow tires. Since we wanted to drive it, we decided to order a set of new wheels and tires. No one makes the original 997 wheels, so we had to go with the later style wheels. They look great, and we know they are safe. The original wheels and caps are included, so the next owner can have them restored. With it finally back on the ground, I got to work buttoning the engine bay up and tuning the engine. While it would start, it didn’t run well. I had cleaned and resealed the carburetors, but didn’t do a full rebuild. After checking for leaks, I discovered the shafts were leaking air, so I took the carbs back off for a full rebuild. New bushings, shafts, and jet hardware were installed. Once I got the carbs back on, I set them to the default settings, and it fired right up, but still wouldn’t rev. I adjusted the ignition timing and started it back up. Once it was warmed up, I used our ColorTune tool and set the mixture on both carbs. It now revs great and idles smoothly.

Since the seat upholstery appears to be original, we decided to retain it, but the carpets were in rough shape. So, I pulled all the old carpets out and painted the floors with POR-15. It appears someone drilled  drain holes in the floor pans, so I installed plugs in them to keep water out. New carpets from Newton Commercial went in with all new pads underneath. I also replaced the rubber gaskets in the doors and rear pop-out windows. The entire interior was cleaned and treated with UV protectant.

Like most Minis from this era, the sliding window channels were in rough shape, so I removed the windows to replace the channels and felts. Incredibly, the drainholes weren’t plugged up or rusted out, so in went new channels and felt. The interior is nice and tight now while going down the road. With the side windows partially opened and the rear windows popped out, it gets great airflow! This car was optioned with the large heater box and blower motor for those cold mornings.

Given how rare and unique these early Coopers are, we wanted to preserve rather than erase the car’s history. I think this side by side comparison of how the engine bay used to look versus how it looks now captures exactly what the goal was. When you open the hood, it’s tidy, but is loaded with character.

Getting this Mini back on the road was a ton of work, but we have been having a great time driving it around. It gets tons of looks everywhere it goes and puts a smile on your face every time you drive it. I’ve lost track of how many hours went into research just so we could keep it as close to the original spec as possible. There are still a few things to do, but they are all minor jobs, like refurbishing the door hinges, adjusting the hood, and replacing the remaining rubber body bits. There’s also some rust in the rear fender liner and in the door bottoms that could be addressed, but neither impacts driving it. We treated these areas with cavity wax, so that things don’t progress. We’ve had our fun with it but a new project is already waiting for my attention, so will be offering it for sale here on Barn Finds soon. Be sure to keep an eye out for it and let me know what you think of the final product!

How it came to us

Restoration Photos

How it looks now

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Comments

  1. ccrvtt

    Awesome! Thanks for sharing the story.

    Like 1
  2. Kent

    997 cu in 4 cylinder???

    Like 1
    • bobhess bobhessMember

      Cubic centimeters.

      Like 0
  3. bobhess bobhessMember

    Great article Josh! Like the way you work.

    Like 0
  4. Jack M.

    Hagerty did a rebuild of one on YouTube 4 years ago. It’s up to 951K views. If anyone else is into Mini Coopers.

    Like 0

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